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Service Case StudyConverting Paper to Electronic Documents (prepared by Niraj Goyal)The work described below was carried out in a large company based in the US and India. The project dealt with converting printed paper from US customers into electronic copies. The material was quite heterogeneous in nature - consisting of assorted magazines and legal papers. It is part of an ongoing operation that services several customers. The results obtained have wide applicability in the back rooms of industries processing large amounts of data - IT enabled services, banks, insurance companies, hospitals etc. - and computer based office processes.This project was taken up as a demonstration example within the framework of building a Six Sigma mind-set in the organisation, while training a core group in the use of the techniques and the teamwork required. The problem solving methodology consisted of seven steps, combined with quality tools to create a dramatic improvement in the quality of the output far beyond the expectations of anyone in the organisation.The narrative unfolds in the same sequence as the project followed - through each of the seven steps of problem solving accompanied by education in and application of the six sigma techniques relevant to the problem.1. Selection Of The Problem1.1 Brainstorming. A meeting of the senior management of the company was held and a brainstorming session produced a list of over 30 problems. These were placed into two categories: “End result problems faced by the external customers Internal problems that were causes of customer problems rather than basic problems themselves.The realisation that the first category of problems was the one to be attacked (customer focus) came spontaneously.Next, prioritisation was done to select the most important problem using the weighted voting system followed by a quick discussion to produce a consensus. The theme selected was Consistency of Quality and Timeliness.1.2 Selecting the problem area: Within the theme, intuitively the management recommended a particular customer line. When asked to collect data for different customer lines and present it, to their surprise they found that another major line had a bigger problem. This was the line selected. Their realisation of the importance of data-based problem solving had begun!1.3 Definition of the problem: Data (including errors) was collected for 30 days. During this exercise it was realised that different auditors were classifying the same error in two different ways, leading to measurement system discrepancies. This led to a reclassification of the errors, and training of the auditors.From the data then collected and analysed the problem was defined as follows: Customer requirement: 50 ppm errors Current process average errors: 510 ppm Variability (sigma): 710 ppm (Average + 3 sigma): 2640 ppmNote: Errors were collected before rework to ensure that the root causes would be exposed.Problem definition: Reduce error density to assure 3-sigma quality under 50 ppm from the current 2640 ppm (i.e. 98%).2. Finding The Vital Few To AttackThe errors collected were categorised using a Pareto diagram. Prioritisation was required at three levels: Level 1: Four categories, C1 to C4 - one category (C1) constituted 85% of the errors Level 2: C1 into 4 categories, C11 to C14 - one (C11) category constitutes 98% of the errors Level 3: C11 into 4 categories, C111 to C114 - one (C111) constituted 85% of the errors Category C111 was attacked as it constituted approximately 65% of the total problem.3. Idea Formulation For CountermeasuresSeven error types were found in C111 in two broad categories. They were examined to determine why each one could have occurred, and a brainstorm for possible countermeasures was done. The most likely measures to Kill the Problems were selected for trial implementation.4. Idea Testing And ModificationThe selected countermeasures were analysed and tested for each error type and the successful countermeasure was short-listed for implementation.5. Implementation Of CountermeasuresTraining instructions were prepared for the new procedures and all the operators were trained. Implementation of all the countermeasures was done across the system from a particular date.6. Confirming The ResultsThe team was trained in control charts and the X bar and sigma charts were introduced to monitor the results. A dramatic reduction occurred from the day of implementation ,and the first three weeks confirmed that a drop of 90% in error density had been achieved from 2640 ppm to around 300 ppm.Tremendous enthusiasm was generated in the team as the result of this project far exceeded their expectation.7. Maintenance Of Improvement - Continuous Small ImprovementsStandard operating procedures (SOP) were drawn up for the process changes. A special session with the operating personnel emphasising regular review, and killing any abnormal peaks that may have occurred in the control chart was explained. An SOP covered the frequency of review meetings for each level of supervision and management and a review format was introduced. The line supervisor who was part of the team became the enthusiastic owner of quality and the control chart, as well as the leader of the team charged with maintaining quality and continuously improving it. The slogan If you do not improve, you deteriorate was introduced.This effort gradually brought down the (average + 3 sigma) error density further from 300 ppm to 50ppm.The Quality Improvement (QI) StoryA QI Story was prepared for presentation to senior management detailing the improvements that occurred:Tangible Customer delight: Customer reported 100% quality in his sampling consistently over six months. He could not find errors at such a low density. Productivity and Cost: Inspection and rework reduced to almost zero. 99.7% first pass efficiency. Sampling sizes were reduced. These resulted in savings of US $ 50000 per annum at Indian wage levels (in US equivalent US $ 300,000 per annum). Volume Increase: Approximately 50% by the customer. The production went through without increased manpower. Turnaround of the documents was improved dramatically due to no rework and started meeting customer requirements.Intangible Senior management time saved Motivation of the operations personnel very high Team work between Operations, Instruction and tool development and QA personnel Mind-set Changes Producing quality saves money The importance of data and six sigma techniques. If you dont improve, you deteriorateFuture plans for improving the turnaround by 50%, using Just in Time methods are being implemented now.Co
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